Actiflo is an enhanced sewage settlement system which uses tilted plate separator
technology and fine sand particles to increase the settlement rate of flocculated
solids. Originally developed as a clarification process for potable water, it
has now been used for the primary settlement of municipal wastewater.
Poor contact
Since the works went into service a number of upgrades have been carried out
to meet Environmental Agency (EA) discharge consents. The main process elements
of the original plant were coarse and fine screening, grit removal, free oil
and grease (FOG) separation, submerged biological contactors (SBC) and final
settlement (FST). Over time it became clear the secondary-treatment SBCs were
under-performing, due partly to problems at the FOG separation stage. In response,
United Utilities sought a solution based on a primary treatment stage in order
to reduce the overall loading on the SBCs.
Three processes were considered, conventional primary settlement, dissolved
air flotation (DAF) and Actiflo. Conventional primary settlement tanks were
ruled out due to a high capital cost of approximately £10M. A DAF unit
was tested but found to be ineffective as a result of the high sand content
in the incoming sewage. A full-scale DAF unit would also mean extending the
existing building, creating planning problems.
A pilot of OTVB’s Actiflo system was set up in a bid to reduce the organic
loading to the SBC’s in various modes of operation. The results demonstrated
removal efficiencies of 60 to 70% in suspended solids (SS), COD and BOD with
up-flow velocities of 100m/h. It was also shown that, after full shutdown, the
process could start up again and operate at full efficiency within 30 minutes.
An additional benefit was Actiflo’s small footprint which allowed retro-fitting
to the existing works, thereby reducing capital costs and avoiding the requirement
for planning permission.
Following the trials, the company won a £2.2M contract to design, build
and commission the full-scale plant. The design principally comprised three
Actiflo units, two Multiflo units, ferric chloride storage and dosing, polymer
preparation and dosing, microsand storage, batching and transfer system, hydrocyclones,
sludge transfer pumps and instrumentation and control.
To minimise capital costs, and avoid the need for planning permission, the
three existing FOG tanks were used to provide the feed tanks for the Actiflo
units. Modifications to accommodate new penstocks, coagulation and flocculation
mixers, baffle arrangements, lamella packs and launders, together with bottom
sludge draw-offs were designed into the existing reinforced concrete structures.
The system incorporates enhanced settlement with very small sand particles
(microsand) used to add weight to the flocculated organic solids. Following
fine screening and grit removal, raw influent enters a coagulation stage where
a primary coagulant, ferric chloride or aluminium sulphate, polymer and microsand
are injected and mixed rapidly. The influent enters a flocculation stage, via
a baffle arrangement, where gentle mixing and further addition of polymer causes
the suspended solids and the microsand to combine forming weighted flocs. Lamella
plate settlers separate the flocs and the clarified effluent passes to the secondary-treatment
stage. Sludge is re-circulated to a hydrocyclone where the sand is recovered
for re-injection into the process. Separated sludge from the hydrocyclone, is
treated in a Multiflo unit and supernatant is returned to the Actiflo inlet.
The Multiflo process is designed to thicken sludge from the Actiflo before
dewatering. It consists of two stages; polymer and ferric chloride are added
to the separated sludge and denser flocs are formed with the aid of a picket
fence mixer. The sludge then passes through lamella settlers where it is thickened
to approximately 4 to 6%. In practice, sludge is consistently being produced
at the upper end of the concentration scale and can be sent directly to the
belt presses, instead of being mixed with SBC sludge and thickened via gravity
belt thickeners. Supernatant, with an SS level below 100mg/l, is discharged
from the top of the unit and returned to the inlet of the Actiflo.
The system’s operating regime is dictated by seasonal differences in influent
characteristics. Maximum flow, biological demand and SS levels occur in winter,
whereas significantly higher levels of FOG enter the STW in summer. The Actiflo
units were therefore designed to take 50% of the maximum winter flow, 4,140m3/h,
during winter – when this is reached flows run directly to the SBCs via a new
bypass channel. During summer, when input does not reach 4,140m3/hour, flows
are processed entirely by Actiflo.
Take-over tests commenced in June and show the plant should meet United Utilities’
requirements and discharge limits set by the EA. The quality of sludge from
the SBCs was also improved dramatically, affording substantial cost savings
on the operation of the existing odour treatment system.
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